Attn: Todd AWE - Update on 17535 & 17537 Fuel Trim Too Rich Banks 1&2
The car ran alot like it did the day when we thought we had everything fixed. Boost seemed to come on a second time around 5k and pulled fairly smoothly, a bit jerkiness up high, I assume this would be the default air / fuel mixture not being just right due to the lack of air metering.
I didn't have a chance to log anything with the MAF unplugged yet. Do you think it's safe to say it's most likely the MAF causing the DTC's ? I assume there could still be a problem with N75 as well, but the MAF seems to be the most problematic at this point.
I will plug the MAF back in and take it for another spin and see if the DTC's return.
Your thoughts ?
Thanks again for all of your assistance, it is much appreciated.



